Tank sensing

- Replace certain fittings with welds inside tank 

 

Aft end cavity environment failure

- Increase fire suppression capacity by 15x

 

Booster leak mitigation 

– Replace certain manifolds with dedicated drain per corresponding valve

Replace certion flanges with better seals and improve joint design

Replace certion fittings with welds in specific location

- Replace accessible valves of a certain type with new design

- Replace certain flange bolts with higher strength bolts and increase torque

- Disallow certain seal re-use, and add cameras to monitor all engines during ground operations

- Increased scrutiny on leak checks 

- 90+ cameras added to detect leakage during operations

 

Raptor leak mitigation

- Add leak capture and drain hardwarev for valves of a certain type

- leak check and screen for porosity on igniter units

- Improved igniter seal design 

- Weld certain alignment bolt holes shut 

- Reassess k-factor and torque for engine hot joint #1, add leak capture and route overboard

- Reassess k-factor and torque for engine hot joint #2 

- Add safety cable to certain fluid lines on high risk locations

- Add one methane sensor per engine bay

- Ground test campaign to better characterize typical engine leakage

- Improve structural FEA/fatigue analysis for all medium to high criticality lines

 

Collateral damage from fire

- Add insulation to engine lines sensitive to thermally driven loads

- Add insulation to avionic harnessing

- Add backup wire to specific harness

- Improve thermal protection of avionics tray

- Change routing to flight computers

 

 

Booster reliability improvement

- Replace sensor with more reliable units

- Coat gimbal assembly with lubricant

- Add pump pressure sensors to certain location

- Add pump temperature sensors to certain location

- Replace certain bolts, and increase torque for certain flanges

- New seal design for certain areas of booster

- Add electric actuation system

- Better manage engine bay pressure by increasing fire suppression capacity by

- Replace sensor with more reliable units 

- Coat gimbal assembly with lubricant 

- Add pump pressure sensors to certain location

- Add pump temperature sensors to certain location

- Replace certain bolts, and increase torque for certain flanges

- New seal design for certain areas of booster

- Add electric actuation system

- Better manage engine bay pressure by increasing fire suppression capacity by 15x

- Change certain booster valve timing 

 

 

Raptor reliability improvement

- Add final leak checks for critical joints 

- Add support bracket for certain sensor 

- Add support bracket for certain sensor 

- Add check valves to certain areas of engine

- Improve oxygen valve design

- Improve oxygen valve seal design

- Improve design of hot manifold

- Change nitrogen shutdown usage

- Change engine shutdown logic

- Increase capability for ground leakage mitigation

- Redesign fire suppression system

- Change conditions around bolts

- Change timing of specific valve actuation

 

 

Avionics reliability

- Eliminate certain type of connector improvement

- Redesign network architecture

 

 

Risk Process

- Improve risk tracking process

 

 

Safety System

- Implement improvements to safety system

- Verify flight safety system design improvements using additional type of test article

- Verify flight safety system design improvements via analysis

- Perform component testing

 

N

- Review and improve operations surrounding flight safety system

 

 

Change Control

- Improve CAD controls

- Add engineering walkdown

- Improve use of change management system

 

Pad Design

-Redesign of launch pad deck

- Improve assumptions for new pad deck design

- Add water cooled pad deck

 

Pad Design Process

- Improve pad deck design documentation

- Improve pad design process


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